Has anybody used this wire
FabCO EXTREME B2
E81T5-B2M H8
I'm having a problem with this burning through tips with in minute of changing it.
mig and flux core tips and techniques, equipment, filler metal
Artie F. Emm
- Artie F. Emm
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Could this be a polarity problem? FCAW is generally electrode negative, while GMAW is electrode positive. Machines vary in how they handle this: some have positive and negative ports on the front of the machine that allow you to jack the leads in as needed. Other machines have polarity switches or settings.
I'm thinking that a burned tip may be the result of power flowing in the wrong direction.
I'm thinking that a burned tip may be the result of power flowing in the wrong direction.
Dave
aka "RTFM"
aka "RTFM"
DCEN is the way it is set up. I have been using this for about 6 month. It has done this from day one and it is getting old. When in am welding it locks like the fix is melting out of the wire before it gets to the puddle. I thank it is going back to the tip and burning the inside of it.
- MinnesotaDave
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Location:Big Lake/Monticello MN, U.S.A.
What are your set up numbers - do they match this chart?
What is your stick-out length?
Is the wire old or new?
What is your stick-out length?
Is the wire old or new?
- hobart fcaw wire AWS E81T5-B2M H8.GIF (39.41 KiB) Viewed 1664 times
Dave J.
Beware of false knowledge; it is more dangerous than ignorance. ~George Bernard Shaw~
Syncro 350
Invertec v250-s
Thermal Arc 161 and 300
MM210
Dialarc
Tried being normal once, didn't take....I think it was a Tuesday.
Beware of false knowledge; it is more dangerous than ignorance. ~George Bernard Shaw~
Syncro 350
Invertec v250-s
Thermal Arc 161 and 300
MM210
Dialarc
Tried being normal once, didn't take....I think it was a Tuesday.
May be wrong here but most dual shield is run EP. Also, do you have knurled drive rolls? If the wire is getting crushed at the feed rolls you wouldn't know until it hits the tip... causing your issue. Check tension and polarity!
I welds bad if it is in DCEP and good in DCEN. I know that is set up the right way. I replace the drive rollers earlier this year they're practically brand new still.
They are just tight enough to barely move through my glove it is also only double roller system.
They are just tight enough to barely move through my glove it is also only double roller system.
- MinnesotaDave
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Joined:Sun Oct 27, 2013 10:57 pm
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Location:Big Lake/Monticello MN, U.S.A.
Man, at this point I think I'd call the wire manufacturer for guidance.
I'd sure be frustrated if it didn't work correctly.
I'd sure be frustrated if it didn't work correctly.
Dave J.
Beware of false knowledge; it is more dangerous than ignorance. ~George Bernard Shaw~
Syncro 350
Invertec v250-s
Thermal Arc 161 and 300
MM210
Dialarc
Tried being normal once, didn't take....I think it was a Tuesday.
Beware of false knowledge; it is more dangerous than ignorance. ~George Bernard Shaw~
Syncro 350
Invertec v250-s
Thermal Arc 161 and 300
MM210
Dialarc
Tried being normal once, didn't take....I think it was a Tuesday.
- MinnesotaDave
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Joined:Sun Oct 27, 2013 10:57 pm
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Location:Big Lake/Monticello MN, U.S.A.
I can imagine - I'd be interested to hear what the factory rep says about the issue.quvit92 wrote:Man it is really getting to me
Maybe it's happened to others and they know what to do about it?
Dave J.
Beware of false knowledge; it is more dangerous than ignorance. ~George Bernard Shaw~
Syncro 350
Invertec v250-s
Thermal Arc 161 and 300
MM210
Dialarc
Tried being normal once, didn't take....I think it was a Tuesday.
Beware of false knowledge; it is more dangerous than ignorance. ~George Bernard Shaw~
Syncro 350
Invertec v250-s
Thermal Arc 161 and 300
MM210
Dialarc
Tried being normal once, didn't take....I think it was a Tuesday.
what do you mean by burning thru tips? burnback? the tip bore has doubled? tips last a long time, when the wire welds to the end of the tip , the tip is not burnt or shot, just needs to to be fixed. Why that happened is what you want to Know. I dont think that you ran 25 lbs of wire thru that tip and wore it out or burnt it out. sounds like a simple mig short circuit welding problem.
tip stick out is too short, burnback setting too short, poor ground , what voltage and wire feed speed caused this problem?
tip stick out is too short, burnback setting too short, poor ground , what voltage and wire feed speed caused this problem?
what I want in the end is strong , clean looking welds, I never attained that with flux core ,never liked it - so I only went to argon-co2 , and with the crappiest equipment , I achieve great results,I use good tips, correct gas and american made mig wire in my crappy welder. Mig welder.Welding is more complicated than you may believe. The equipment only needs to supply the power and decent wire speed ,correct gas and consumables IMO. weather short circuit welding or spray transfer. I make an analogy .I have a cheap Chinese band-saw that works good , but I had to modify it to work to my expectations , made new legs, welded some supports on the guide rollers -bla-bla-bla and use only american made blades. For me it was wort the the time to dial in the saw for my home-owner use. So what I'm saying is, focus on your end results and use the best practices and to achieve that goal
within your budget
within your budget
- MinnesotaDave
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Weldmonger
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Joined:Sun Oct 27, 2013 10:57 pm
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Location:Big Lake/Monticello MN, U.S.A.
Ah, still had smooth wheels from hard wire in the machine.quvit92 wrote:So I got is fixed it was the rollers the one on the right is what I had in the machine and I switch to the black one on the left it works perfectly now
So it would slip a little occasionally and melt the wire to the tip - that would explain it.
Now it probably feeds easy and reliably - glad it's fixed for you man
Dave J.
Beware of false knowledge; it is more dangerous than ignorance. ~George Bernard Shaw~
Syncro 350
Invertec v250-s
Thermal Arc 161 and 300
MM210
Dialarc
Tried being normal once, didn't take....I think it was a Tuesday.
Beware of false knowledge; it is more dangerous than ignorance. ~George Bernard Shaw~
Syncro 350
Invertec v250-s
Thermal Arc 161 and 300
MM210
Dialarc
Tried being normal once, didn't take....I think it was a Tuesday.
that is possible and true .stick with quality products that You are comfortable with. the end results should be consistent with your expectations. Use the best , premium products recommended . Wire choice can make a world of difference! I can not recommend any wire brand of flux core as I prefer gas shield.
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